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| I own a Ryobi Weed Trimmer, gas powered about 3 years old. The model number is 725R. It is the model that has a few different attachments that can be used with it. I have the weed trimmer and blower attachments. My problem is this: The trimmer line always spins (slips) back into the head which forces me to shut the unit off, unscrew the head and the re feed the trimmer line into the head and wind it up again. This happens everytime I use this thing. I have the right size diameter line and am following the line installation directions exactly as stated. I'll be trimming along and will let the trimmer idle for a moment while walking to another part of the yard and when I rev the engine to start trimming again the line disappears into the head. I can not bump feed this unit either. I spend more time re loading the line than I do trimming. Is this happening to anyone else, or is it just me? I don't get it. If you know of a way to keep the line from doing this, or a replacement head that will not do this, please let me know. Thanks,
Jeff |
Follow-Up Postings:
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| Jeff one thing I have noticed about my Ryobi trimmer is that if any weeds get wrapped around the shft it pushes the head down towards the nut and the spool doesnt lock into place and the automatic feed doesnt work. I have to occasionally stop and clean the shaft off above the head. If that isnt a problem then Im not sure what the answer is. |
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| I also had - note past tense - the same problems with my Ryobi "Grass Scopion" line trimmer Model RCT2800A. I got so frustrated with the line spooler/head problems that, after a few years, I would have rather used a pair of hand shears to do the lawn edging! Considering that 2-stroke engines are pretty good now-a-days, I would argue that the trimmer head is the most important functional part of a line trimmer. However there are some very good trimmer heads available that ARE designed to do the job, e.g. from Stihl et. al. When looking for the leader* in 'design', the number of patents taken out is generally a good indication and, going by the number of patents taken out by Ryobi, I ended up buying a good aftermarket head for AU$50, and it's made in Australia to boot. **Another problem I had to fix on the Ryobi was a sticky throttle. Initially I thought it need a tune up because I didn't have the throttle control I expected Lampet |
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| I have several Ryobi trimmers. The line feed mechanism works fine with the standard line. It almost sounds like you have your line wound backwards. Think about it - it goes back into the head and you can not use the bump head. Just try reversing the direction of how you wind it. |
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- Posted by fruitjarfla (My Page) on Sun, Jun 4, 06 at 8:13
| A TV garden guy suggested spraying the spool with vegetable oil. |
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| I should have mentioned that the original trimmer head on my Ryobi "Grass Scorpion" was of the single spool type, and that the aftermarket one has a split spool. With the Ryobi (single) spool, I always made sure to wind on the (paired) lines in the direction of the arrow that was moulded into the plastic and always kept the total length of line less that 2 metres (i.e. 1m for each side) in an attempt keep the wound spool as tidy as possible. In operation however, tangles inevitably occurred on the spool. In any case, it always seemed to me to be very optimistic to expect two lines - wound on as a pair onto a single spool - to feed out smoothly through the opposing exit ports of the head without ever crossing over each other and creating a tangle. If you have a split spool in the head of 'your' Ryobi and you are winding the line on in right direction (as marked?), then it should feed the line out at least as good as my aftermaket split spool type. Lampet |
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- Posted by boodgie2shoes (My Page) on Wed, Aug 1, 07 at 14:50
| I have had this issue as well. Thanks for all of the very good suggestions. Unfortunately, I still had the same issue where the line simply would not spool out. So, I spent awhile looking at the thing, and this is the solution I came up with that works for me: The bump knob screws into the spool assembly with a reverse thread screw. The screw is held into the bump knob with a washer that seats into the plastic inside the knob. There is a bit of slop because of this, which in my case meant that the bump knob screwed down too tight onto the assembly. And that prevented the spool from moving inside the casing. Solution: Unscrew the bump knob and add an extra washer to the bolt (one should do it, but you may need two) Works like a charm now. Also my 2 cents on winding the line: make sure the line is wound on the spool fairly tightly, and try to make sure the pair of lines stay together. That should help prevent the line from getting bound up in the spool. |
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